Today’s case study is a 2002 Mini Cooper S

This one came to me for a very intermittent no start.  The customer has been driving it like this since he purchased it a few months ago.  It was becoming more frequent lately.

I was called to check it out at his work. The car would crank over but wouldn’t start. The S model is super charged and it requires an hour’s labor just to check fuel pressure and it also requires a special adapter that is Mini specific. I didn’t want to waste an hour of this customer’s money to check fuel pressure. I gave the intake a shot of fuel and the car started and died. I told the customer it will require a fuel pump and a fuel pump relay.

After leaving, the customer called me back and said his car now starts and runs again. Before I left, we discussed the issue with the pump and the most likely cause of this condition. The customer was unsure of my finding, but he decided to trust me and ordered the fuel pump and relay. The parts came in and I decided to current ramp the old fuel pump before removing it. This would allow me to show the owner what I was talking about and why I didn’t want to remove his super charger’s inter-cooler to verify that the fuel pump pressure would have issues, too. Here’s the waveform using my Pico Scope. As we see in this image, the amperage draw from the pump is 5 amps higher than normal. We also see that the commutator segments are showing poor contact at the brushes. We see the pumps RPM’s are low by almost 3000 RPM’s.

It’s clear the pump is bad. The high amperage and low RPM’s are part of the cause of this intermittent no start complaint. The pump’s brushes have poor contact with the commutator segments and are losing the ability to rotate the armature at startup. This causes the intermittent no start problem and explains why it can sometimes still start and run. The low RPM’s will cause low fuel pressure. This can and will cause other driveability problems. This one had 2 stored DTC’s, a P0300 and a P0302. Replacing the pump also corrected these 2 DTC’s without needless replacement of other parts.

Pico Scope Waveform

This customer is very happy and even called me later to thank me for fixing his car without needing to replace unnecessary parts. He was also happy because we didn’t need to waste money with prolonged diagnostic work by removing the super charger’s inter-cooler to verify that fuel pressure was also an issue.

Sometimes there are better ways to do things and this was just such a case. I always recommend that you know who is working on your car and if they’re qualified to do the work, do it properly without wasting your hard earned money.

2013 Ford Explorer No Start

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The Snap-On Verus Pro was able to read all the stored DTC information.

This one was towed in as a no start. The customer had it into another shop and they diagnosed it as a bad starter. After the starter was replaced it had the same problem. They had it towed to another shop and that shop called me to diagnose the vehicle. I do a lot of electrical work for this shop. The vehicle didn’t crank over when the key was turned to the start position. I noticed the DIC was displaying a message for a starting system fault. The other shop told the customer the vehicle didn’t have any codes. I hooked up my Snap-On Verus Pro and found 3 DTC’s in memory. 2 for the PATS anti-theft system and 1 for an ABS fault.
My only concerns were the 2 PATS fault DTC’s. It was necessary to hook-up my Ford factory scan tool to read the key data PID’s for the PATS system. When the key was inserted into the ignition lock cylinder the data PID never switched to key present. I had the shop call the customer to bring down the spare key to see if it was a key problem. The spare key was unable to be identified by the PATS system as well. This lead me to remove the center stack with the radio and heater controls as well as the dash speedometer cluster to gain access to the ignition switch. It was necessary to remove the ignition lock cylinder/switch assembly for testing.

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The PATS anti-theft system transceiver that reads the key’s transmitter ID information.

It was necessary to check fuse F18 and back probe the transceiver. This is a check for the PCM wake up request from the ignition lock cylinder when the key is inserted into the cylinder.
Both the fuse voltage and the wake up request signal were present. The next step was to verify the circuit ground. Without being able to crank the starter to load the circuit, I could only measure it with the PCM wake up command request. The ground looked good and gave correct battery voltage on the load side from the PCM.

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Wiring diagram for the Transceiver, BCM and PCM circuits.
Notice the lack of signal information in this schematic. It’s
yet another reason to have the proper tools and education
to properly diagnose today’s complex vehicles.

 

I used my Snap-On Vantage Ultra to perform a frequency test to measure a change in the signal inputs to the BCM in an attempt to check the transceiver’s ability to send the key input signal to the Body Control Module. It’s also known as the BCM.

The factory diagnostic information does not offer internal module and signal information. Without knowing what the signal actually is, I tried a few different signal tests and only managed to get the frequency signal to respond. The RX signal had no response and the TX signal had 2.60 hz output. I still didn’t know the proper signal info, but with one side unable to respond to the BCM it was necessary to order a replacement transceiver. Unfortunately, Ford and other manufacturers never give internal module control input/output signal information.

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After the repairs the stored DTC’s were cleared and did not reset. This verifies that the repair is complete and the system is 100% functional.

The new Ford transceiver was delivered and installed. The data PID was able to read both keys as present and the vehicle started up without a problem. After installing the transceiver and putting everything back together, I found a PCM update available for this vehicle and the customer was okay with updating his car after fixing the no start problem.

The replacement transceiver signal was 7.85 hz on both the RX and TX circuits to the BCM. This case study will go into my fixed repair files for future information for the next one that has this problem.

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After the transceiver was replaced and everything was put back together the vehicle starts and runs without any further issues.

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After the repairs were completed, the customer authorized a PCM update to the latest software calibrations. This insures proper vehicle operation and eliminates possible software related faults that can’t be fixed by throwing parts at it. No guesswork here!

This is another case study that shows why proper tooling is necessary to diagnose today’s computerized and high technology vehicles.
Code readers can’t give you the information required to do the job right. Throwing parts at the car is a complete waste of time and money. Don’t waste your time and money on guesswork repairs. Find a skilled technician with the proper tools and education to fix it right the first time.

2009 Ford F150 Random No Start

The BJB is the main fuse relay box

The Battery Junction Box – They managed to break every mounting post to get the box opened.

This one came to me through another shop. The customer is a regular patron of the referral shop, but they didn’t wanna tackle it. They are not equipped for this type of work and know better than to take on something like this.  The customer had it into a shop elsewhere out of town and they sold him a $1000.00 PCM to try and fix a random no start.

It was referred to me and I found a lot of damaged wires, broken BJB mounts, pinched wires and general poor workmanship all over this one. They replaced a relay, the PCM and hacked the wire harness trying to resolve this problem. They never managed to find it and after spending $1500.00 plus, the customer was not sure it could ever be found.

Replacement PCM didn't fix it

The new PCM

I came to the customer’s residence and set up my diagnostic systems and started by looking at the factory wiring diagrams. The fault was traced to the load side of the relay they replaced. Without testing the control and source side of the circuit they decided to throw the best guess and most expensive part at the problem. They guessed it was the PCM that was causing the problem and never tested it’s ability to control the relay before spending $1000 of the customers money on it. They guessed WRONG!

I wish I could afford to spend money like that…. Can you afford to ?

The cause of failure

The COF  This simple fuse problem was overlooked. The fuse was overheated from high resistance in the BJB. The simple 12-volt basics were overlooked and guesswork won out.

After looking at the wiring diagram, I quickly found the source of the intermittent no start problem. The fuse was getting hot and the contacts were burnt. The contacts had reduced contact tension which caused a loss of power after the vehicle was driven and allowed to get up to operating temperature. The BJB is in the engine compartment and above the radiator. This would cause expansion and contraction from the temperature changes. These changes would cause the fuse to drop voltage across the terminals and result in a no start condition. After sitting for a few hours it would restart because the contacts were able to carry the voltage and amperage when the BJB would contract after cooling off. It would complete the circuit and the truck would start again.

The BJB is part of the wire harness and it carries a price tag of $1100.00 with a 3 to 4 hour replacement time. It’s a lot of work and an expensive repair for such a minor issue. Imagine the shock from being told this after you wasted $1500.00 on guesswork repairs that didn’t fix anything. Now you need to spend another $1500.00 for the correct fix. That’s double the cost due to unskilled guesswork by uneducated non-professionals.

In reality, this was done by a so-called Dealer Technician. This doesn’t really surprise me as I see this type of work way too often. It’s a recurring pattern in my field.

I was able to correct this problem without the need to spend that $1500.00 on the replacement BJB by moving the circuit to another fuse port in the BJB.  Needless to say the customer was very happy to have it fixed and without spending needlessly. I also did a current ramp test of the circuit to verify it wasn’t an over amperage problem on the load side of the relay. The fuse is on the feed side of the relay and the original fuse never blew. The amperage test  on this 20 amp circuit shows the circuit only pulls 9 amps and is well within the operating threshold specifications.

This Case is closed and with another happy customer. 

Fuel Gauge Problems

This one came to me after the customer became frustrated with the shop that sold her a fuel pump. She had been back to the shop 3 times with fuel gauge problems after they installed the fuel pump. She told them the gauge was inaccurate and wouldn’t read full when it was filled at the gas station. They were insistent the fault was with the gauge on the dash and wanted to sell her a cluster to correct the problem. This one wasn’t cheap. 700 bucks total was the replacement bill. She decided not to have them do the work because she didn’t have any problems before they replaced her fuel pump.

After some preliminary inspection it was necessary to remove the fuel pump to inspect the installation work. WOW!  What a great job. They knocked the fuel level float assemble off of the fuel pump housing. The float was just lying inside the tank moving around at random. It’s not a wonder she had a problem, but 700 bucks would not have corrected this one. Sloppy workmanship was the problem and the shop wasn’t even willing to double check the work they did before condemning the dash cluster.

What a wonderful job they did. Can you afford to waste 700 dollars that won’t fix your car ? This is the result of unskilled labor and sloppy workmanship….

Guess who has to pay to have this problem corrected. Don’t let this happen to your car. Find a qualified technician to work on your car or it could cost you a lot more than you ever expected. Don’t let unskilled labor cost you unnecessarily. 20150205_102248

As you can see in the picture this was caused by someone in a hurry. They didn’t even take the time to check their work and didn’t care about the job they did. The fuel level float was completely knocked off the fuel pump housing. This is not the type of work you want to pay good money for. Then be charged another 700 dollars to try and fix something they caused because it’s easier to throw parts at it than it is to diagnose it. Anyone can hack and butcher a car. Don’t get ripped off by unskilled labor.

1998 Buick LeSabre No Code Diagnostic 3.8L V-6

Today’s vehicle is a 1998 Buick LeSabre. The customer had taken it to another shop for a Service Engine Soon light and a hesitation on acceleration. The SES lamp was not on when she took into the shop. They couldn’t pull any codes and told her they couldn’t diagnose her car without codes, after having it for 2 days. They charged her 120.00 dollars and told her if the light comes back on, they would look at it again.

Needless to say, she was very unhappy and wasn’t willing to play games with them, that’s when she called me. I assured her I would be able to diagnose her car with no codes, as long as I could verify her complaint. She gave me the chance to look at it. I took it out for a road test and noticed it was misfiring under load and backfiring through the intake.

These are the misfires that were captured during the road test with the GM Factory Tech 2 scan tool, under heavy load.20131127_132211It was necessary to hook up my GM Factory Tech 2 scan tool and re-road test it. I found a steady misfire from cylinder #6 and some random misfires from cylinder #3. I came back to the shop and started a diagnostic strategy based on my findings. This lead me to inspect the ignition system and it’s related components. I was shocked that the other shop was unable to help this customer with her car. They should have at least tried.

This car has a DIS ignition system. It’s a waste spark design.  Cylinders 1-4 share a common coil, as do 6-3 and 5-2.  It has 3 coil packs and 1 control module.  The spark plug wires looked fairly new and the # 6-3 coil had recently been replaced. The customer said that she had work done last summer in 2012. When I did my diagnostic inspection, I found the coil towers for cylinders # 1-4 and 6-3 were heavily corroded.  The spark plug wires were also corroded and the wrong spark plugs were installed. The corrosion problem has damaged the plug wires and both the # 1-4 and new 6-3 coils. Whoever did the work last year failed to use dielectric grease on the plug boots. Moisture accumulated unchecked under the plug boots and corroded the towers and plug wires until it caused high resistance between the coil towers and plugs wires. They could no longer conduct the high KV required to operate the spark plugs during heavy demands on acceleration.

The corrosion on the coil towers.20131127_134916This was a simple no code diagnostic problem and was created by poor workmanship.

If the previous work would have been done right the first time, this would not be a costly and troublesome issue now. The lack of workmanship caused more damage than it fixed. Fix it right the first time and save money. Letting an unskilled person work on your car will cost you double and your vehicles reliability will be lost. Don’t be a victim of unskilled labor.